This is what I had with mine - an original connector on the white/grey wire at the 'W' terminal had gone - the wire core had snapped just behind the crimp that holds the insulation on the wire and the insulation had hardened so it looked fine with no movement - it wasnt untill I applied pressure along the wire (to lengthen/shorten it) that I was able to match the movement to the tacho's odd behaviour (needs 2 folk to do). I soldered on a new connector with cover and all has been well since..........